Fish'n Jim wrote:
If the crank was at spec, then must be low miles? Odometer reading?
I suspect since it was not a wear issue, that maybe one or more valves or rings were stuck giving the "0" compression and may have avoided a rebuild. ie; it had to turn over to get those figures. No signs of cracks or other causes/leaks were noted.
Starting fresh is good, no issue, just curious. My '49 odo was around 45K, reportedly sat 5 years, and it ran just fine after resurrection. Took about a month to get it all repaired. Slight valve noise in need of adjustment but idled nicely and quietly at 400 with no overheat. Glad I didn't tear motor down. I was deciding whether to restore or hot rod. I drove it around the neighborhood for a while before tearing it apart as it sits.
Wish I had your enthusiasm.
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