Re: Headliner installation on '53 Packard
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Not too shy to talk
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will i checked every thing over and found that i did have the wiring hooked up backwards due to i went to a neg. ground. the wire from the relay needs to be hooked up to the #4 terminal and the wire from the kick down switch need to go to the #6 terminal. it will be the other if i stay with the pos.ground. i took the car out and in over drive i can get up to 70mph and the alt. light did not come on. and every thing semes to be working real good now. i have to say thanks for all your help i real do appreciate it...
thanks again joe in tn..
Posted on: 2010/4/24 12:11
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Re: Headliner installation on '53 Packard
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Not too shy to talk
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thanks for the reply.
do you know the best way to check for this. and if the sol. is still in pull-in how do you repair that. is there a chance that i have the wires hook up backwards. there is one wire coming from the kick down switch and the other is from the relay on the fire wall. as the best that i could i rewired the car to factory. only change was going to a neg. ground due to i installed a 12v battery in the trunk to power the am-fm radio in the trunk. which it turned out pretty good.. thanks for the info. joe in TN..
Posted on: 2010/4/23 14:52
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Re: Headliner installation on '53 Packard
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Not too shy to talk
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hay to all
i know this started out as a headliner question and ended up as a charging question. will i had the old girl out to day and found out that the gen. light comes on with the over drive ingauged when i get up to abount 50,55mph. i can turn the over drive off by pulling out the knob and go 60 to 65mph and the light will not come on. any though on what it could be or how i can check out each part in the electricel sys. on the over drive unit. now i can say that i do think the over dive is working due to the engine is not turning as many rpm. and when i let off on the gas pedal the car gose into a cost mode and reingaugs when i press. the gas pedal. thanks for any help joseph in TN..
Posted on: 2010/4/23 9:08
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Re: 327 exhaust header stright 8
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Not too shy to talk
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will you have a good point there. it will save me a lot of money. and you make it sound easy. i may try that.
joe
Posted on: 2010/4/5 18:29
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Re: Headliner installation on '53 Packard
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Not too shy to talk
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no you do have it right is the battery post to the gen. and i checked that is what i did. joe
Posted on: 2010/4/4 18:58
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Re: 327 exhaust header stright 8
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Not too shy to talk
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will if i can find somebody i think it will look real cool. i may try my local muffler shop i don't know. joe
p.s. think god for spell check
Posted on: 2010/4/4 17:22
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Re: Headliner installation on '53 Packard
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Not too shy to talk
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yah i took a jumper wier and shorted out the battery post and the field on the voltage rag.. i think it's the field will the one in the middle next to the battery post on the voltage rag. i think thats right. joe
Posted on: 2010/4/4 17:13
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Re: Headliner installation on '53 Packard
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Not too shy to talk
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will i went with the neg. ground due to i mounted a 12v radio in the trunk and it is neg. ground i did not went nothing to short out. know when i went to the 6volt neg. ground and did change the voltage reg. and changed the wiers in the coil. all gauges, light and overdrive are working good. and the engine starts real good. so i thank there is something out of adjustment or the original gen. may be going which it looked good when i took it apart to clean it up. joe
Posted on: 2010/4/3 19:24
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Re: Headliner installation on '53 Packard
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Not too shy to talk
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no not yet i did take it out for a short drive today.for the first time. mostly i have just driven it around the naberhood. car did good i did have the battery light on when i got up to 55mph i slowed down and the light went out. so i will have to find out what is going on with the 6volt neg. ground set up that i have. other then that it all went well. joe
Posted on: 2010/4/3 18:47
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